I guess yesterday was to good to be true because today didn't go quite as planned.
It started quite well, I fitted the brake pipe for the rear brakes, I originally thought that I had lost the fitting for the connection yesterday but today with the spotlight on I realised that there wasn't one and that the copper just screwed onto the flexy via the bracket. Which leads me into the first problem of the day; I moved onto the front calipers which went on and connected up without a problem and looked great.
It was when I took the photo I realised that there should be a bracket bolted on so the brake pipes are secured, I checked thru my photos of when I stripped it and there was the bracket.Original bracket |
I have searched everywhere for them and they are gone without a trace, I think they may have been left at the powder coaters when I put my first lot in a couple of months ago. It was easy enough to get around this as there was no chance of me driving all the way to the coaters, so I made a couple of new ones, unfortunately its the nuts that are also missing that's the problem. Bet they turn up when I'm not looking.
One of the new brackets |
New bracket fitted |
The next job was pretty straight forward and went without a hitch and that was to finish blasting the rear drums and give them a light spray to try and keep the rust at bay for at least a week.
Brake drums |
That's the last of my designed one's fitted and if I had the money I would have had a mold made of both sides of the upper arms because what I thought was a scale drawing from Floflex wasn't.
This was a bit of a disappointment when I opened the pack but the biggest was yet to come.
I had to decide whether to see if I could return these and have a red face plus the fact I would have to figure out what else to order or I could try altering them. After yesterdays success and realising just how easy this poly is to alter I thought I would give it ago.
The sizes I required are:-
38mm OD instead of 46mm.
36.5mm between the flanges
44.5mm overall width instead of the 65mm.
As I no longer own a lathe I decided upon a vertical drive to spin centrally so attached the bush to my drill in its stand via a 12mm bolt with spacer washers borrowed from my bench grinder.
Bush fitted to vertical drill |
This kept the diameter perfectly parallel and the size (I thought) came out perfect at 38mm, unfortunately a huge dose of stupidity lent a hand.
What a great accomplishment turning down a poly bush by hand to 38.09mm, think again!
I had forgotten to take into account the tightness of the bush on the spindle which as the bush got hot needed tightening a little more and a little more to stop it spinning. So great, success until I tried to fit it in the axle bush hole and found it over a mil to small, I couldn't believe it. After doubling checking my sizes I realised that as it was tightened it squashed up and as I released the nut it returned to its correct diameter.
Well you have to laugh.
I still have the other bush to do, so I will check the size by loosening the nut and allowing to cool before taking a measurement, of course I will have to buy another bush, that will be £10 for the bush and £8 postage.
Well over £200 for the rear bushes so far. £80 for the Teflon blank and the mold, so really only around £120 about the same as the front.
I had to give up after this disappointment so got the brush out and cleaned up.
I hope to get a little more done tomorrow but that will be my last day as I am off early Sunday for a 17 day trip this time, hopefully I will have a full 2 weeks off when I return, although we find out about redundancies at the end of the month so I may have more time than I thought to work on car.
See ya Paul
No comments:
Post a Comment