Tuesday 17 July 2012

Kallista Manual

Hi
Well, I have been rather busy lately but unfortunately it has not been much on the car, mainly because I have been waiting for the head to arrive and yesterday I got an email  from the Car Clinic to say it is ready. I am having it unleaded and it also requires the valve guides renewing and a skim, bit of a problem now as I am back to work at 0230 in the morning so a little to late, so I have arranged for them to hold it until I return.

I have been getting a few small jobs done on the car but my time has mainly been spent on the computer studying courses for my new job.
Yes time to move on, so last Wednesday I went for an interview in Great Yarmouth on the Norfolk coast, bit of a journey as I set out at 0615 and got home at 0130 the next day rather tired but successful so this is my last trip on the DFDS Dover ferry service. 
My new company is called Seajacks, one of the newest and most innovative in the offshore wind farm and oil and gas installation business. The ships are self propelled dynamic positioning jackup ships, difficult to explain but a picture speaks a thousand words.
The ships sails to its location, positions itself using its dynamic positioning system then;
Drops its legs and lifts itself out of the water to give a stable platform with no rocking from the waves.
It can then build or repair the wind turbines or oil gas platforms.
Pretty amazing ships, so I have been rather busy studying every day.

One thing that did arrive was my new engine paint, the same company as the black paint for the heads and paints on nice and smooth with great colour.

I have at last got hold of the Bruno spares catalog and just as importantly the Work manual for the Kallista, up until now I have been working blind but hopefully now I should get a few thing right. I was told by Bruno that the spares cataogue was on the disc supplied by Geli from the Panther club so I sent her an email and quick as a flash the disc arrived. Great disc packed with info, photos and more importantly the spares and workshop manual.
All printed and bound with well over 350 pages.
While everything is apart again I thought I would try to explain what went wrong with the gearbox extention.
I thought, as other people who have been in contact with me thought; that because the extension is designed for a type 9 gearbox that it would fit and work with any Ford setup, well it don't.
It all has to do with the position of the knuckle joint, if the spline'd connection tube was a few inches longer and the knuckle set back then no problem but the design of the Panther drive shaft is all wrong for this extension, again a picture speaks etc!
You can see that the position of the knuckle is perfect to hit on every pass.
I have even made a little video to show you.
So to make it work requires a re-design of the drive shaft to set the knuckle back which even though I really wanted the space in front of the gearstick I don't think the expense is worth it.
Well not a lot accomplished on the car, the damage to the head really set me back both financially around £400, and time wise.
I have just had my SORN reminder and have re-sorned the car, so that is 1 year I have been working on the car but due to my work patterns that is really only 6 months.
So next time home I will hopefully be able to get the head on and engine /gearbox fitted before I go on holiday and start my new job.

see ya Paul

Tuesday 10 July 2012

Bearing Shells

Hi
Well not much to write about as progress is slow while waiting for the parts to arrive.

I have managed to get a few bits complete, all of the pistons have been removed and cleaned and replaced everything was fine with these. They just required a spray and clean where a little of the emulsified oil had gotten into the shell.
The main bearings shells were also in great condition although the oil way's around the wasted bolts were full of black sludge so the removal was a very good idea.
These are all spotless now and the oil passage ways have been oiled and blown through.
You can see the small amount of oil on the shell and that was about it.

I also removed the most rear cap even though I had it off to refit the sump gasket and oil seal, this was because before deciding to remove the engine I had thought about trying to remove the damaged piston in position and to do this I had to remove the sump pan. Two things I learn't while under the engine is that I had an oil leak from around the rear of the sump, this could be from either the gasket leaking, the new oil seal leaking or from the interface of the rear bearing cap not sealed correctly. The other thing I found out is that you can't access one of the sump bolts next to the curve around the rear oil seal, it is just impossible to get a socket in position you can't even get a socket on while the engine is turned over on the stand never mind under the car. So the engine had to come out, although this effort did make life a lot easier.
Once everything was cleaned up I used most of a tube of my new Hylomar blue on sealing the cap interface, around the outside of the oil seal and under and over the sump gasket.
I had thought that maybe the sump gasket may have been the source of the leak and because I was using a old style sump pan without the buttons on to keep the gasket from squishing out I though I might have a go at repairing the original pan. I had a couple of sticks of silver solder lying around for years so I begged the use of some oxy acet gear and after giving the area a good grind I silver soldered the holes and the general area.
After a water test that held Ok I think I'll chance it. I have also got hold of a tin of Rust Bullet resin paint so I rubbed down the whole pan an give it a coat. When it was dry last night I gave it a coat of Stone chip.
The gasket and bearing cap was fitted and torqued down to 95Nm then with plenty of blue hylomar, the oil pump then sump pan was put on and tightened, I have made sure to take it easy and not let the gasket squeeze out by over tightening.
I am still waiting for the engine paint to arrive so until then I made do with just the prep work for painting, plenty of gunk to get all of the oil off and a good rub down with a scotch bright and wash down. I have also removed what I can and painted separately.
Not much else I can do until the head arrives, I have had confirmation that they are working on it and hopefully it will arrive before I return to work.
I have fitted one of the heads, after cleaning the faces and double checking that nothing has dropped inside.
This is the new gasket, I have fitted the head over unit 5, out of sight out of mind.
I have not torqued it down yet and shall wait until both heads are on before I do that, guess I'll just have to wait.

see ya Paul

Saturday 7 July 2012

Fitting Piston

Hi
More deliveries today and my new / used piston was one of them.
The new one is on the left of the photo, just a little oilier and a lot less damaged.
I was just going to use the crown from the new one and use the original conn rod but after trying to remove the gudgeon pin I soon realised that it had been pressed into the rod and unless I used a lot of brute force it was not coming out. I had asked when ordering the piston if I could have the piston from unit #5 because of the number stamp just in case I had to use it, I checked the part numbers and everything matched so after a good clean up in it went.
I did not have the correct ring compressing tool for fitting the piston so a little imagination required, well a couple of worm clips.
Plenty of oil and the bearings went in and torqued per the Haynes manual to 31 Nm or as near as I could get.
After fitting the piston I oiled everything up and gave the engine a turn. I then decided that as unit #5 had a lot of oily rust in the bore then maybe the rest have, so all of the pistons are to come out and all crank bearing caps are to come off.
After the first piston came out I am glad I decided to pull them.
The piston is a little cruddy but the rings still have movement so with the oil additive they would / maybe have cleaned up. Anyway a little bit of elbow grease and it cleaned up nicely, unfortunately I also do not have a ring expansion tool so instead of risking breaking a ring I just left them in place and sprayed plenty of WD40 into the groove and cleaned as best I can .
The bores were also a little cruddy.
So the rotary wire wheel and a good rub with the diamond paper and they came up nice.
I have only managed 4 units today and will carry on tomorrow and get everything spotless.

til tomorrow

see ya Paul

Friday 6 July 2012

Engine damage

Hi
Back again and 2 weeks away to think about my broken little engine, when I say little this is what I am used to working on.
You really make sure no spring washers are left in these baby's intakes or it may cost a few hundred thou and a trip home.

I have managed to gather the new parts together although only the head gaskets have arrived, I had a good look at the air manifold gasket and because of the minimal torque and the quality of the gasket material I have decided to re-use it, not so with the heavy torque on the head so a new set have arrived. I was going to buy the same gaskets by Payen but I came across a set of Ford original 2.8 Cologne by Reinz for around £28, I looked up Reinz before buying and they also are a high quality manufacturer so good enough for Ford then good enough for me.
The head is at the Car Clinic and was supplied by Tickover for around £55 inc delivery they have also supplied me with a few other pieces in the past and have been very helpful, I reckon the total for the head will be around £300. The piston is from a Capri and I bought this from a guy on eBay for £11 inc delivery, and he says it in fair condition so hopefully I'll just need to change the conn rod and piston rings and all should be good.

I tried to get started yesterday morning but after having a good look at the damage and draining the oil I just didn't have the get up and go to get started, don't know if I was more angry at myself for it happening or upset about it so I packed it in for the morning and went out to buy the bits I'm going to need. I went and bought another 5 litres of 10w40 and engine flush from Halfords, came home, kicked the dog and felt a whole lot better so got to work. It was mostly prep work getting ready to lift the engine/gearbox out again, so back up on the stands; exhaust first followed by the drive shaft followed by clutch cable etc. I refitted the heads and exhaust manifolds with the lifting straps fitted and any other bits removed so it was ready for today's lift.
All of the prep work paid off as today it was just a matter of rigging the hoist, taking the weight and removing the mounts. The jack was positioned under the gearbox and I lowered the engine onto the trolley.

I then lowered the rear of the car onto its wheels and rigged the lifting straps to the front and lifted the car with the hoist until I was able to pull out the engine, hope nothing else goes wrong but if it does I'm getting to be a dab hand at this fitting removal business.
I was now able to lower the car and push it outside so as to rest the engine on the workbench and remove the gearbox, clutch and flywheel.
The engine stand that had been dismantled and stowed in the shed had to be rebuilt then the engine mounted. I remember I foolishly wrote in my last blog that I didn't think any water had gotten into the sump, well how wrong can a person be, it may not have been much but it had certainly emulsified so after removing the sump pan a lot of cleaning was necessary, luckily because I had not turned the engine on the stand before removing the pan hardly any had gotten into the engine itself and had remained in the sump. The pump was dismantlement as that was full and the sump strainer removed and cleaned.
A lot of cleaning required around the flange area to remove the old sealant but not much else it seems.
Now for the bit I had been dreading, on first inspection when I found the damage it did not seem to have affected the bore to much now it was time to find out. I removed the bottom cap, the bottom shell and tapped out the piston, it was a good job I had bought another piston as the damage is worse than first thought.
Defiantly a deceased piston, the first ring is a little tight as the crown has been squished a little but I have managed to move it and it should remove easily enough. Its £86 plus vat and p+p for a full set of rings so I am hoping to reuse the ring set as there does not seem to be any damage to the top ring.
Once I had inspected the piston I plucked up the courage and turned the engine, the bore was a little rusty and dirty from where the water had been so a rub with a scouring pad and some diamond wet and dry to clean it up and the spotlight was put on it. I am a very very lucky boy as apart from a few chip to the very top of the bore the inside seems not to have been damaged.
So now I just have to wait until the head and piston arrive before I can rebuilt and refit, a lot of cleaning first as the engine is covered in oil and dirt so a good clean, rub down and repaint while I am waiting.
While away and after a number of emails from Terry B I have found out why the engine would not start, for which I am very grateful or the damage would have been much worse. 
It would appear I made a rather bad mistake on piping up the fuel system, when I took the picture of the fuel pipes they had been moved out of the way to remove the engine.
This moving made the pipe from the fuel regulator (the pipe with the white tape) look like it was coming from the fuel filter to the regulator and that the loose pipe with the pipe protector was from the fuel pump to the carb. Well this is the way I fitted them, wrong!! the way it works is fuel filter to the fuel pump inlet (protected pipe), out of the fuel pump to the regulator inlet, out of the regulator to the carb and the return from the regulator back to fuel tank. Simple. Also the carb return had been blanked internally which you can't see and I was never told so I followed the instructions for the fitting of the carb which states to pipe for the carb return goes to the system return and Weber supplies the tee to do just this. Wrong again, thankfully.
So when it is all back together and correctly piped up it should start first time, I wish.
Some other good news, my TVR Griffith seats have arrived and look great if a little grubby, after all they are 20 years old. I had a go at one of the headrests with a little saddle soap and a rub with conditioner and it has come up lovely, once I clean all of the leather and re-colour them they will look like very clean 20 year old seats.
The cleaned headrest is on the right also the frames need a little work but that's no problem.

Well that all that got done today.

see ya Paul